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Thread: The scrounged Cadet

  1. #1
    ggggr's Avatar
    ggggr is offline part time super hero and seeker of justice
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    The scrounged Cadet

    I have recently scrounged a Bsa Cadet action off here and a stock as well from someone else. The piston is with my neighbour to weld up a bit of wear just behind the cocking slot. I've made a piston washer ready for when it comes back and fitted a DCL Dave breech seal in the barrel. I cleaned the bits up and decided to "borrow" a piston out of another gun today. I cut 2 brass 1BA screws to size for the front stock scews (should be 7/32 BSF-----but 1BA is very close and should be ok with them being brass) and found a 2BA for the rear stock screw. I put the action together with the spring that came with it as I cannot find a Cadet one here. I tried a couple of shots from just the action and it barely shifted a pellet. I decided to try blowing down the barrel to see if the breech seal was leaking. A lot of air could be heard. I then put my fingers over the stock screw holes and the air leak stopped! It is actually leaking from the left stock screw. I don't think someone has forced a screw in and I don't think it is leaking from round the thread, like a Webley Hawk I did years ago. I think the thread has gone too deep and maybe just touched the transfer port wall. You cannot see anything by shining a torch down the cylinder and poking something into the screw hole.
    The good thing is it does not seem to leak when the stock screw is in. I may end up putting some gunge in the bottom of the hole-------or try a bit of tube in the transfer port to see if that stops some leakage-----just out of curiousity.

    When I got the action in the stock, it didn't want to cock, partly as the trigger was catching on the guard and partly due to rubbing on the slot in the stock. A few touches with a file seems to have sorted it out. I'll attempt a plink if the weather is ok and await the return of the piston so I can refit it.
    Cooler than Mace Windu with a FRO, walking into Members Only and saying "Bitches, be cool"

  2. #2
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    enjoy it bud

  3. #3
    ggggr's Avatar
    ggggr is offline part time super hero and seeker of justice
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    Getting there. I still need to wait for the original piston to come back and then sort it out.
    As I thought one stock screw had just broken into the wall of the transfer port, I tried to epoxy a bit of aerial into the the port but i think most of it came off as I was pushing the bit of aerial in. So i tried to put a bit of epoxy in the screw hole and put a screw in to try to persuade the epoxy to seal where it needed to seal. I then took the screw out and cleaned any residue off.
    I put the gun together late afternoon and it still didn't always fire a pellet, which I think was partly the breech seal gripping the pellet and partly a grubby barrel (maybe the piston washer a bit tight too?) . Anyhow after good barrel clean and easing the breech seal it started to plink well. It is shooting a fraction high and left but grouping really well. I'll leave the sights until after I've refitted the original piston.
    There is a slight kick to the gun, which might be either a tight piston washer, or the bit of aerial in the transfer port needing to come out--------even though the port still looks fairly big.
    I don't think it is an under powered mainspring--as even though I'm not sure what it is, has a bit of pretension on it.

    Has anyone ever tried to sleeve a Cadet port? I only really tried it to stop the air leak.
    Cooler than Mace Windu with a FRO, walking into Members Only and saying "Bitches, be cool"

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